Marjol Battery Site
 
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Stormwater Management System

 

STORMWATER STRUCTURES

In order to control stormwater at the Site both during and after construction activities and to keep sediment (small soil particles that are carried along in water) on the Site and out of the Lackawanna River, a basin and other drainage features such as check dams and swales were constructed as outlined in the USEPA/PADEP-approved 100% Design Plan for the Site (Click here for more information on the Final 100% Remedial Design Plan). The stormwater management system consists of several items
(Click on the name of the structure to view a picture of the structure):

1) Swales - to direct the flow of water on the Site to the sedimentation basin.

2) Check Dams (elevated rows of rocks in the swales) – constructed to slow the water down as it flows through the swales.

3) Sedimentation basin – designed to hold water from a 100-year storm; rainwater that falls on the Site is directed to the basin where sediment will settle out prior to the water being discharged since water from areas without grass yet that drain to the basin may carry sediment. Once the remediation at the Site is complete and grass is growing, the basin is converted to a stormwater management basin.

4) Baffle - a fence with fabric on it to slow down the water in the basin after it comes down from the swales and allow additional sediment settling. 

5) Skimmer - when water is released from the basin, it is released through a skimmer which is a 4-inch plastic tube that skims the water off the top of the basin and into a discharge pipe. The water then flows out through the discharge channel and into Sulphur Creek.

6) Outlet structure – water from the basin flows through the skimmer and into the outlet structure which discharges the water into the discharge channel via a pipe to the opposite side of the basin berm.  (Click here to view a picture of water discharging from the outlet structure.)
    

 

STORMWATER SAMPLING AND DISCHARGE

The 100% Design Plan calls for stormwater from the clean areas of the Site to be collected in the new temporary sediment basin. Sediment that is carried along with the stormwater settles out in the basin, and stormwater collected in the basin is released to Sulphur Creek under a permit issued by the State of Pennsylvania. During construction of the Final Remedy at the Site, the drainage system is designed so stormwater falling on contaminated areas of the Site does not flow into the basin, but is retained within the contaminated areas by berms.

If there is not enough space for all of the water to be held within the contaminated areas, however, the design provides for the potentially contaminated water to also drain to the sediment basin. Since lead sticks to the sediment, as long as the sediment is kept on the site by allowing it to settle out of the water in the basin, the water can be safely discharged to the river. This sediment can then be easily excavated and placed into the Containment Area before the final cap is installed. In this way, the water is managed so that the lead remains on the site by controlling where the sediment goes.

Sampling of the basin discharge is included in the 100% Design Plan and became part of the state permit. The design requires stormwater from the basin to be sampled as it is being discharged into Sulphur Creek until the areas draining to the basin have grass growing on them. The basin stormwater sampling plan consists of the following:

  1. Collect real-time information that can be used for timely action – The water discharge from the basin is sampled using a turbidity meter. (Turbidity is the amount of soil particles in the water. Since lead sticks to the soil particles, if there is low turbidity in the water, then there will be, at most, a minimal amount of lead in the water.) The water is sampled every day that water is discharging from the basin. The turbidity meter provides instant information on the amount of sediment that is being released. The turbidity information is used to determine when to take immediate action.

If the skimmer has been raised so that it does not discharge water (for example, if there is a concern that contaminants may have entered the basin), then the basin water is checked to see if the turbidity is above the performance standard of 250 NTUs. If it is above 250 NTUs, then a flocculant (i.e. Pond Clear) is added to the water to get the soil particles to drop to the bottom leaving clear water at the surface. Once the turbidity is below 250 NTUs, the skimmer is lowered and the basin water discharges through the skimmer. (Click here for a picture of the skimmer in the discharge position.)

  1. Collect lab data on stormwater – Samples of the discharge water are taken at least monthly and analyzed for total and dissolved lead to confirm that contaminated material is not discharging from the basin. (Click here for a picture of water discharging from the basin at the discharge point along the perimeter fence.)

 

STORMWATER DISCHARGE INFORMATION JULY 19, 2010 to AUGUST 2, 2010 INCLUDING DISCUSSIONS ON DISCHARGES ABOVE THE PERFORMANCE STANDARD

On July 19, 2010, a heavy rain event (approximately 0.35 inches in 1 hour) occurred at the Marjol Battery Site (Site).  The heavy rain eroded areas of the Site that were not yet stabilized with grass or erosion control materials.  Due to the erosion, the stormwater that flowed through the north and south swales and into the basin was turbid and caused the discharge from the basin to exceed the turbidity standard.  Flow from the basin was stopped as soon as the exceedance was observed.  During the days following this initial turbidity exceedance, Gould diligently worked to enable discharge from the basin to occur within NPDES permit turbidity requirements.  Several measures were taken to control the turbidity in the sedimentation basin including the addition of several hundred pounds of a flocculant (Pond Clear), placement of Floc Logs (used to remove sediment from water), and the placement of geotextile around the skimmer head (as an additional filter).  On August 2, 2010, water in the sedimentation basin became clearer allowing discharge from the sedimentation basin to take place and continue without exceeding the turbidity standard. 

Since July 19, 2010, nearly all areas of the Site have been stabilized which should prevent the kind of turbidity that occurred in the basin on July 19, 2010.  Gould will continue to monitor the flow into the basin and the discharge channel throughout the next few storm events to ensure that the basin discharge is below the turbidity standard. 

Water samples (analyzed for total and dissolved lead) were collected at the discharge point during the initial July 19, 2010 turbidity exceedance and also during an exceedance on July 21, 2010.   The dissolved lead results were all below the laboratory detection limit of 1.0 ug/L.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L.  There is not an NPDES standard for total lead, but the total lead result will be compared to the turbidity levels and then to the dissolved lead results.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river.

USEPA, PADEP, and Throop Borough were kept informed on stormwater management activities during the period from July 19 to August 2, 2010.  A formal non-compliance report covering the period from July 19 to August 2, 2010 was submitted to PADEP on August 4, 2010.  (Click here to review the July 19, 2010 Non-Compliance Report.)  See below for a description of the daily stormwater management activities for the period from July 19, 2010 through August 2, 2010:  

July 19, 2010 - On July 19, 2010, after a heavy storm in the late afternoon (over 1.5 inches of rain was received on July 19, 2010), there was a stormwater discharge above the performance standard.  The skimmer was in the discharge position in accordance with the Stormwater Management Design Plan.  After the heavy rainfall, AGC took a turbidity reading at the discharge point and the turbidity meter gave an “Error” message indicating that the levels were above the range of the instrument.   (Turbidity is a measurement of the cloudiness of the water which is caused by sediment.)  The skimmer was flipped to discontinue flow from the basin and a flocculant (Pond-Clear) was added to the basin to enable the sediments to settle out of the water to the bottom of the basin.  Samples of the discharge were taken for the monthly total and dissolved lead analysis.  The dissolved lead result was below the laboratory detection limit of 1.0 ug/L.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L. The total lead result was 368 ug/L. There is not an NPDES standard for total lead, but the total lead result will be compared to the turbidity levels and then to the dissolved lead result.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river.

July 20, 2010 - On the morning of July 20, 2010, between 7:13 AM and 7:40 AM, the water in the basin appeared clear, and several readings were taken on the western side of the basin as follows:

69.8 NTU, 116 NTU, 92 NTU, 120 NTU, 122 NTU, 83.8 NTU, 99.1 NTU, 92.7 NTU, 117 NTU, and 89.8 NTU                                   

Based on these readings, the skimmer was flipped at 8:28 AM.  After water reached the discharge point at the perimeter fence, two readings were taken at the fenceline at 8:40 AM.  The results were 61.4 NTU and 79.0 NTUs.  The 200 NTU standard was checked as well and read 197 NTU. In early afternoon, AGC checked the basin again.  The basin and the discharge appeared turbid.  The skimmer was again flipped to stop flow.  Additional Pond Clear was added to the basin to further expedite sediments settling out of the water. 

July 21, 2010 - On July 21, 2010, additional turbidity readings were collected in the basin between 3 and 6 inches below the water surface. All readings in the basin were in the 40 NTU range. Based on these readings, the skimmer was flipped to allow discharge from the basin.  Turbidity readings were once again collected at the discharge point immediately following discharge form the basin. Visual observations at the discharge pipe showed clear water consistent with the basin readings. However, the initial turbidity reading was 290 NTUs.  After one minute of flow, the turbidity reading at the discharge point dropped to 190 NTUs.  It is possible the initial 290 NTU reading at the discharge point was due to sediment within the discharge channel.  A third turbidity reading was collected at the discharge point 10 minutes later; the reading was 140 NTUs. Approximately a half-hour later the discharge turbidity reduced to 16 NTUs.  Based on these readings, discharge was allowed to continue with periodic monitoring until approximately 45 minutes later when the turbidity increased to 390 NTUs.  The skimmer was then flipped again to prevent discharge form the basin. Further investigation revealed that the basin water is clear in the top few inches, but below that the turbidity is much higher indicating the Pond Clear is working, but that additional “doses” are needed.  Samples for total and dissolved lead were collected on July 21, 2010.  Two sets of samples were collected: one when turbidity was low and one when turbidity was high.   The dissolved lead results were both below the laboratory detection limit of 1.0 ug/L.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L. The total lead results were .91 ug/L and 38.3 ug/L, respectively. There is not an NPDES standard for total lead, but the total lead results will be compared to the turbidity levels and then to the dissolved lead results.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river. 

Note: Due to questions on the accuracy of the initial turbidity meter being used, a second meter was sent to the Site and is being used to check the accuracy of the original meter.

July 22, 2010 - No discharge took place from the sedimentation basin.  Additional Pond Clear was added to the basin on July 22, 2010.  

July 23, 2010 - On the morning of July 23, 2010, ten turbidity samples were collected in the sediment basin.  The turbidity readings were all well below the performance standard of 250 NTUs, with the highest result being 30.7 NTUs.  Therefore, the skimmer was flipped to allow discharge from the sedimentation basin.  A turbidity reading was collected at the discharge point shortly after discharge; the result was 161 NTUs.  A turbidity reading collected 10 minutes later was 92.1 NTUs.  The basin was checked approximately every hour throughout the day with all readings being below 65 NTUs until about 2 pm when the turbidity readings began to increase (97.6 NTUs at 2 pm and 181 NTUs at 3 pm).  Due to the increase in turbidity in a short period of time, the skimmer was flipped to stop discharge from the sedimentation basin.

Additional flocculants (Floc Logs) were then added to the check dams and in the basin to assist with settling out the sediments from the basin.  There was no additional discharge from the basin on July 23, 2010. 

July 24, 2010 - On the morning of July 24, 2010, ten turbidity samples were collected in the sediment basin.  The turbidity readings were all well below the performance standard of 250 NTUs, with all results being below 50 NTUs.  Therefore, the skimmer was flipped to allow discharge from the sedimentation basin.  A turbidity reading was collected at the discharge point shortly after discharge; the result was 124 NTUs.  The discharge was monitored frequently and at approximately 7:40 am, in response to a turbidity reading of 177 NTUs, discharge from the basin was stopped.

After allowing additional time for sediments to settle out, the basin was re-evaluated in the afternoon.  Turbidity readings were again collected in the sedimentation basin; all results were below 75 NTUs.  The skimmer was therefore flipped again to allow discharge from the sedimentation basin.  A turbidity reading was collected at the discharge point shortly after discharge; the result was 73.5 NTUs.  The basin was checked approximately every half hour throughout the rest of the day with all readings being below 100 NTUs.  At 5:40 pm discharge from the sediment basin was stopped for the weekend. 

July 25 to July 27, 2010 - No discharge took place from the sedimentation basin.

July 28, 2010 - On the morning of July 28, 2010, ten turbidity samples were collected in the sediment basin. The turbidity readings were all close to the performance standard of 250 NTUs, so the skimmer was flipped (9:00 am) to allow discharge from the sedimentation basin. A turbidity reading was collected at the discharge point shortly after discharge (9:08 am); the result was 752 NTUs, so the skimmer was immediately flipped to stop discharge from the sedimentation basin.

Additional flocculant material (Pond Clear) was then added again to the sedimentation basin to assist with settling out the sediments from the basin.

July 29, 2010 - On the morning of July 29, 2010, ten turbidity samples were collected in the sediment basin. The turbidity readings were all close to the performance standard of 250 NTUs, so the skimmer was flipped (11:20 am) to allow discharge from the sedimentation basin.  Turbidity readings collected at the discharge point just after discharge were just above the performance standard (highest being 300 NTUs), so the skimmer was immediately flipped (11:30 am) to stop discharge from the sedimentation basin.

July 30, 2010 - Geotextile was placed over the skimmer head to act as an additional filter for the water prior to discharge. The skimmer was flipped at 11:25 am. A turbidity reading of 309 NTUs was immediately collected at the discharge pipe (309 NTU) and the discharge was stopped at 11:29 am.  Additional fabric was applied over the skimmer head and discharge was again initiated at 2:40 pm. Three turbidity readings at the discharge pipe were collected (254 NTUs, 274 NTUs, and 281 NTUs). The turbidity at the discharge point was 166 NTUs. Six more turbidity readings were gathered at the discharge point over a span of 25 minutes with an increasing trend toward but not exceeding the performance standard. At 3:20 pm discharge was discontinued after a turbidity reading of 249 NTUs was collected.

July 31, 2010  - No discharge took place from the sedimentation basin.

August 1, 2010 - No discharge took place from the sedimentation basin.

August 2, 2010 - Discharge from the sedimentation basin was initiated at 7:30 am based on visual observations of the water in the sedimentation basin. The observations clearly showed a reduction in turbidity in the basin and clear water was observed to at least a 1-2 foot depth. Discharge was permitted to continue after a reading of 48.3 NTUs was collected at the discharge pipe. Six turbidity readings were collected at the discharge point throughout the morning with results all well below the turbidity standard (highest result was 53.9 NTUs). The monthly discharge sample for August for total and dissolved lead analysis was collected at 11:20 am. The turbidity at the time of sample collection was 6.36 NTUs. The sample results will be available on this page as soon as they are available. 

USEPA, PADEP, and Throop Borough were kept informed on stormwater management activities during the period from July 19 to August 2, 2010.  A formal non-compliance report covering the period from July 19 to August 2, 2010 was submitted to PADEP on August 4, 2010.  (Click here to review the July 19, 2010 Non-Compliance Report.)

 

STORMWATER DISCHARGE ABOVE THE PERFORMANCE STANDARD - MARCH 30 and 31, 2010

Over 1.5 inches of rain was received on March 30, 2010.  The skimmer had been flipped to prevent water from leaving the basin.  (Click here for Stormwater Sampling and Discharge information)  When SCE and AGC representatives checked the Site in the evening during the rain event, there was flow coming from the discharge pipe due to a leak in the skimmer arm.  AGC took a turbidity reading at the discharge point and the result was 77.5 NTUs at 7:30 pm.  (Turbidity is a measurement of the cloudiness of the water which is caused by sediment.)  The basin had filled up to the point of almost going over the baffle, so AGC representatives flipped the skimmer to allow water to discharge from the basin.  Shortly after flipping the skimmer, AGC checked the turbidity at the discharge point.  The turbidity was 330 NTUs at 8:45 pm.  The turbidity level is supposed to be below 250 NTUs for discharge, so AGC flipped the skimmer back into the closed position to stop water from flowing into the discharge channel.  There continued to be some flow in the channel due to the leak in the skimmer arm. 

On March 31, 2010, a turbidity reading was collected at the discharge point at 8:45 am.  The turbidity result was 330 NTUs. A turbidity reading of 324 NTUs was collected at the discharge point at 9:30 am after additional BMPs (hay bales) were added in the channel outside the fence.  Turbidity at the confluence of the discharge channel and Sulphur Creek was checked as well.  Two turbidity readings were taken at this location: one was 152 NTUs and the other was 158 NTUs.  This demonstrated that while compliance with the performance standard was not achieved at the discharge point, it was met before the water entered Sulphur Creek.  As requested by AGC, SCE plugged the skimmer orifice inside the outlet structure around the skimmer orifice plate.  Once the plug was in place, flow into the discharge channel was reduced by approximately 90%.  AGC observed that by approximately 1 pm, all flow in the discharge channel had stopped.   

Water samples (one for total lead and one for dissolved lead) were collected from the discharge point and were sent to the laboratory for analysis.  The dissolved lead result was 4.4 ug/L.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L. The total lead result was 33.9 ug/L. There is not an NPDES standard for total lead, but the total lead result will be compared to the turbidity levels and then to the dissolved lead result.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river.

The skimmer and orifice were repaired during the week of April 5, 2010, to prevent further leaks into the structure.

USEPA, PADEP, and Throop Borough were notified of the turbid discharge.  As is required, a non-compliance report was submitted to PADEP on April 6, 2010.  (Click here to review the March 30, 2010 Non-Compliance Report.)

 

STORMWATER DISCHARGE ABOVE THE PERFORMANCE STANDARD - MARCH 14, 2010

As required when significant rain events occur, on March 14, 2010, AGC personnel conducted an Erosion and Sedimentation Control Inspection at the Marjol Site. The water in the basin and the discharge from the basin was turbid. A turbidity (a measurement of the cloudiness of the water which is caused by sediment) reading was taken for the water being discharged. (Click here for Stormwater Sampling and Discharge information). The water was found to have a sediment load well above the performance standard: 1275 NTUs when it is supposed to be below 250 NTUs. AGC pulled the skimmer to stop discharge from the basin. SCE was called to the Site and applied Pond Clear in the basin and the discharge channel (to cause the sediments to drop out of the water). A leak was found in the outlet structure so water was still able to discharge but at a much slower rate and at a much decreased volume. After the Pond Clear was added, the discharge turbidity dropped to 205 NTUs.

The high flows of water in the discharge channel had blown out the silt fence and silt socks at the fence line, so SCE also placed additional silt socks outside the fence in a U-shape. When AGC left the Site on March 14, 2010, the turbidity levels in the discharge channel had dropped to 195 NTUs.

Water samples (one for total lead and one for dissolved lead) were collected from the discharge point and were sent to the laboratory for analysis.  Dissolved lead was not detected at a detection limit of 1 ug/L.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L. The total lead result is 18.2 ug/L. There is not an NPDES standard for total lead, but the total lead result will be compared to the turbidity levels and then to the dissolved lead result.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river.

SCE worked on March 15 and 16, 2010 to repair the leak in the outlet structure. Once the outlet structure is repaired, the discharge channel will be allowed to drain and then repairs will be made to the silt fence and silt socks. Hay bales were also placed on March 15, 2010. A turbidity reading was collected at the discharge point on March 15, 2010; the result was 223 NTUs.

USEPA, PADEP, and Throop Borough were notified of the situation on March 15, 2010. Lackawanna County Conservation District was also notified. As is required, a non-compliance report was submitted to PADEP on March 19, 2010.  (Click here to review the March 14, 2010 Non-Compliance Report.)

The skimmer was lowered back down on March 16, 2010 to allow water from the basin to drain as it is designed to do. Turbidity readings after the skimmer was lowered were as follows:                  11:30 am - 124  NTUs             11:40 am - 71.8 NTUs

 

 

STORMWATER DISCHARGE ABOVE THE PERFORMANCE STANDARD - JANUARY 25, 2010

As required when significant rain events occur, on January 25, 2010, AGC and SCE personnel conducted an Erosion and Sedimentation Control Inspection at the Marjol Site. During the inspection, they noticed that the water leaving the basin had much more sediment in it than normal. In taking the daily turbidity (a measurement of the cloudiness of the water which is caused by sediment) reading, (click here for Stormwater Sampling and Discharge information), the water was found to have a sediment load well above the performance standard: 1785 NTUs when it is supposed to be below 250 NTUs. Upon investigating , they observed that the skimmer head had separated from the skimmer arm and the arm dropped below the surface of the basin allowing sediment-laden water from the bottom of the basin to be discharged through the outlet structure.

An additional turbidity reading was taken at the discharge point (2183 NTUs) and a series of turbidity readings were collected in the discharge channel, Sulphur Creek and the Lackawanna River.
                                        At the confluence of Sulphur Creek and the River: 119NTU, 116NTU
                                        Sulphur Creek below the discharge: 168 NTU, 145 NTU, 112 NTU
                                        Sulphur Creek at the discharge (rip rap): 1840 NTU, 1918NTU
                                        Lackawanna River below Sulphur Creek: 132 NTU
                                        Sulphur Creek above the discharge: 93.9 NTU, 90.0 NTU
                                        At the discharge point from the Site (fence): 2183 NTUs

Water samples (one for total lead and one for dissolved lead) were collected from the discharge point and were sent to the laboratory for analysis.  The dissolved lead analysis showed a very small amount of lead in the water (0.094 ug/L).  The laboratory sample that is used to determine whether there is contamination of the instrument or something else in the laboratory also showed about the same small amount of lead in it, which means that there was no detectable level of dissolved lead in the discharge water from the site.  The NPDES permit standard for maximum dissolved lead for the Site is 650 ug/L. The total lead result is 64.4 ug/L. There is not an NPDES standard for total lead, but the total lead result will be compared to the turbidity levels and then to the dissolved lead result.  The very low total and dissolved lead results provide reassurance that even though the turbidity levels were above the performance standard, there was NOT a release of lead from the site that would affect the creek or the river.

It is believed that the freeze/thaw in the basin caused the skimmer head to separate from the skimmer arm. A site inspection had been performed by AGC on January 22, 2010 and the skimmer head was attached correctly at that time and the basin surface was frozen.

SCE repaired the skimmer on January 26, 2010. Dewatering through the skimmer resumed once the skimmer was repaired.  AGC collected the following turbidity readings to document that the water at the surface of the basin that was being discharged was below the 250 NTU performance standard:
                                        At discharge pipe – 59.9 NTUs
                                        At discharge point from the Site (fence) – 65.1 NTUs
                                        In basin: Range from 35.8 to 84.5 NTUs

USEPA and PADEP representatives were on Site on January 25, 2010 and notified of the situation. Throop Borough was notified on January 25, 2010 and its Compliance Liaison was on Site on January 26, 2010. Lackawanna County Conservation District was also notified. As is required, a non-compliance report was submitted to PADEP on February 1, 2010.  (Click here to review the January 25, 2010 Non-Compliance Report.)

 

CONTAINMENT (CAP) AREA OVERFLOWS

As a result of heavy rains in July and August, 2009, water overflowed the Containment (cap) Area (CA) (which has contaminated material in it) into a drainage feature (the South Swale) outside of the CA and into the basin on July 31, August 10, and on August 12, 2009. While every effort has been made to keep this type of overflow from occurring, the possibility of it happening was considered in the design, and so the overflow water flowed into the sediment basin as it is supposed to do where the lead contaminated sediment could settle out before the water is discharged. Tests conducted after the overflows show that the discharges were well below the limits that were set by the State to protect the Lackawanna River.

When each of the overflow incidents has occurred, the skimmer in the basin has been raised (if it wasn’t already) to prevent the flow of water from the basin through the discharge channel. Water in the basin was tested for turbidity and when it was below the performance standard, the skimmer was lowered to allow water to discharge.  After the overflow in July, the basin water was also tested for total and dissolved lead. Any sediment and battery casings that have floated onto the CA berm and into the swale were removed and placed back into the CA. XRF analysis (an XRF is a portable instrument used for testing lead concentration in substances such as soil) for lead has been performed on the berm and in the swale to see if the overflow contaminated any previously clean areas.

If the soil lead levels were above the cleanup level, then soils on the berm and swale were excavated and placed into the CA. The excavated areas were rechecked with the XRF to be sure lead levels were below the cleanup standard.

After the first overflow, a meeting was held to discuss how to better control an overflow if it happened again. In order to get more room to hold the contaminated water so that it would not go off-site, it was decided to pump the contaminated water from the CA to a strip pit that was previously excavated – Area B – instead of back into the CA as the practice had been. Area B will be tested near the end of the project and will be re-excavated if necessary with any contaminated material being placed in the CA and solidified. Subsequent efforts after the overflows focused on making sure that the pumps were ready when rain occurred during the night and that the pumps could handle all of the water. While the overflows are not what we would like to see, the important point is that the lead is being contained within the site as it is supposed to be while we are managing the water as best we can with the unfavorable weather we have been having.

Reports with the details of the overflows have been submitted to EPA and DEP. Click on the links below to review the reports. 

Report on July 31, 2009 Overflow                                Report on August 10 and 12, 2009 Overflows

                                                                                                                                                                      


Daily Stormwater and Sediment Data and Information – July 2010

Click on the shaded dates (the numbers) below to view turbidity data, stormwater discharge data and XRF sediment testing data available for those days. (Note: Turbidity data is only collected on days when the basin is discharging or following an overflow of the Containment Area. Collection of samples of stormwater discharge for laboratory analysis is required monthly and has also been performed when overflows have occurred. Sediment sampling has taken place when overflows have occurred.) No testing was performed and therefore no data are available for the dates that are not shaded.  (There was no flow from the basin into the discharge channel for the period from June 18, 2010 to July 19, 2010.)  

 

 
July 2010
S M T W T F S
 
      1 2 3
4 5 6 7 8 9 10
11 12 13 14 15 16 17
18 19 Discharge Above Performance Standard 20 Discharge Above Performance Standard 21 Discharge Above Performance Standard 22 23 24
25 26 27 28 Discharge Above Performance Standard 29 Discharge Above Performance Standard 30 31
                                                                     June 2010                                                                        August 2010  
 

  

Page Last Modified Wednesday September 15, 2010 12:54:29 PM

 

 

 

 

 

 

 

 

 

 

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